Update,
Mileage, 60608
Idle jet confirmed 55
Main jet Confirmed 180
Emulsion tube, 60z lowest 2 holes soldered shut.
power jet 0.65 mm
float .032 washer
No choke plate
Boost 10.738 lbs.
Well, I haven't done an update since I received an order of new emulsion tubes and an adjustable main jet that was made by Bugpack for the Formula Vee cars according to the instructions that came with them.
I checked out the adjustable main jet which came in the original packaging...
....and after hunting for a correct sized o-ring at the local True Value store I got it installed. The funny thing about this adjustable main jet is that it would not work on a Solex 34 pict but it worked fine on the Bocar 34 due to the different way that the main jet sits in the bottoms of each individual carb.
Here is the Jet installed in the Bocar.
I was soooo excited to get what I had thought was the jet to end all jets that I never bothered to check it's size. I installed it and set it to 2 full turns out thinking it would get me close enough to run. I also grabbed the 60z emulsion tube and promptly soldered the two bottom holes shut and stuck it in. I also pulled the power jet and drilled it from a 0.50 mm to 0.65 mm figuring that would get me the rich upper end I needed so bad.
Got it fired up and warmed up and took her out to go fast!!!
Well, As soon as i took off on the main road I saw it go full lean and thought WTH!!!! hmmmmm the main needs to turn out a bit. I pulled off the road and since it was dark I had to hold the flash light and try to get my fingers in there....Oh yeah... and a wrench

.... and try to loosen the lock nut and then turn the jet out another two turns.
Here is a pic that doesn't show the difficulty real well but you get the idea. The idle cut-off solenoid really makes it tough to get in there.
I kept getting interrupted by good neighbors and strangers asking if everything was o.k. since I had all the lights off when the key is off and I was working in the dark.
I tried it again and it was still lean!!!! Stopped the buggy, got out and gave it two more turns which put it at a full six turn out now. Tried it once more and it was still lean.
I headed back home and pulled the 50 idle and tried the 55 idle to see if that made a difference. It helped a bit but it was still lean like the main jet was too small. I couldn't even rev it high enough to see if the power jet came in at 4000 rpm and helped the top end.
Time to go back and think about it. The adjustable main seemed to drip fuel a bit so I didn't want to leave it in there. I pulled the carb and put in the 170 main jet with the 60z air jet and went and tried that.
Pig rich 9.5 to 1 at 2500 rpm to high cruise. It would lean out to 14.5 to 15 to 1 at over half throttle with load in third gear. Full throttle would go full lean at 17 to one at anything over a few lbs. of boost.
Obviously my thinking was going in the wrong direction. Everything I do will not richen up the high load high boost areas. The emulsion tube just makes the mid range pig rich so that is not going to help.
I got the best mid range and high boost with the 170 main and the 75z air jet/emulsion tube.
I decided to leave the 170 in and the 60z in and drive it to work for a few days.
The weather has been getting considerably cooler in the last few weeks so the drive to work in the early mornings have been quite brisk due to the temps being in the low 40's and the last couple days down to freezing. Needless to say I am wide awake by the time I get the 11 miles to work. This is with a light pair of gloves on and my normal work attire which consists of a t-shirt, light flannel shirt, carhartt jeans (sometimes insulated) and my high visibility vest. Since I have a lot of hair I don't ever wear a hat.(makes my head itch

)
The last few days have been raining so I had some time to think everything over and come up wit ha new plan.
I pulled the 170 main out and decided just for the heck of it to check it and a few other jets I have with my new set of wire gauge drills. It turns out that my 170 main was not a 170 main after all

... it was marked 170 ... but the drill showed it to be a 180.
Before a week or so ago I had no way of checking the sizes so I guess I can't be too hard on myself. I also check the adjustable main and what do you know!!!!!!

..the max size the hole was ended up being a 165 main.
No wonder it was running lean at 6 turns out. I also checked the needle and when it is six turns out it is completely past the inlet holes and is just another 165 main jet.
So, I have a couple thing to try after this frustration.
I need to figure out how to get the upper end richer without making the mid range pig rich. I think what I should try next is a bigger main like a 190 or a 195 and then put a bigger air jet in it. That would lean out the rich main at mid range which is where the emulsion tube comes on and if I solder the lower holes shut it should go full rich at full throttle.
It is worth a try.
I have dropped my boost down to 10.5 lbs. to try to get enough fuel at top end but that seemed to make little difference at this time.
I have the carb off and I am going to install a 195 main and a 125z air/emulsion tube with the lower two holes soldered shut and see what happens. I am also going to reinstall my carb top with the choke plate since it needs more fuel when it is this cold out. That should ease my warm up times a bit.
If the weather holds for tomorrow I should be able to test it after work.
I have managed to catch my wife's cold now and feel a bit under the weather, if it doesn't improve I will have to wait a day or two.
Stay tuned
Clonebug