Damn, it died before it ever got installed into a car! 34 dyno hours and not even a clutch drop!


I have not seen this since the last 1500 H case that died about 10 years ago... AS 41 don't do this(it has but damn sure not this easy)... Hell this sucker is no better than a 1500 case!
When Brent spotted this as we were taking the engine off the dyno this morning I had a smile from ear to ear.. it was a sinister smile.
Mission accomplished!
Well, not all the way I'm gonna install it in the blue bug and go finish it off! Its not leaking oil yet so it must still have some life in it that I can wring out..
Crazy thing is that hot it still holds over 150 PSI compression all the way around..The engine sustained head temps over 450 degrees alot of the time with crappy systems and the #3-4 bank has seen over 520 for a short while. Those seats moved a tad bit but still seal off!
I'm gonna drill a hole on either side of the crack. (it goes all the way to the bottom of the case clear to the bell stud on the bottom of the 3-4 bank) and then use some Devcon Titanium putty on that sucker... We'll see how long it takes to start leaking or snap off the rest of the way....
Its time for hell to begin!
I KILLED IT!!!! YES!